storm
Member
I just changed plugs to ngks, taylor wires, new cap/ rotor (detriot tuneup kit)hoping to fix idel miss. no dice started looking ,Well of corse if it can go wrong it will. 1 new wire was assembled poorly and was arcing out of the boot to the heat sheild on the maifold. cut the end off a brand new wire and put a spare accell end on I had around. great idels better but still not perfect. ( I could be expecting to much) went for a drive anything above 10 psi and it breaks up bad, (did not do this before) Ok I saw the coil was original and looked suspect(slight corrosion on terminal) so got a new oem GM one along with a new module. Still same thing. Now after reading I see I sould be around a .30 gap. I have mine set to .35 as this was the reccomend spec I got from a local performance shop that told me my ing had plenty of power and the .35 would make a nice big spark for good burn. Guess they are wrong. I'm done with it for today but will post what happens after tighting them up to .30 sometime tursday just lost ambition for today.
stock truck with KB ram air intake and I deleated the factory muffler with a straight pipe.
stock truck with KB ram air intake and I deleated the factory muffler with a straight pipe.